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Date: Mon, 24 Jul 2023 23:38:00 GMT

Sticky Bottom

Exhaust still not finished.

     Hi all, So why are we still here? Because this harbor has a sticky bottom. Every time you try to leave something get's in the way. So We've gone back and fourth to Dania beach twice a week for the last 3 weeks with the exhaust. We went back today hopefully for the last round. Sections 1-2-3 are in and complete with the exhaust elbow. The muffler is in and we are waiting on the final weld of the muffler end of section 4. It's a piece of art and US Metal Fabricators in Dania beach has done a wonderful job. But they are not fast.

     Sam and I got the prototype back 2 weeks ago and did a test fitting. So that meant taking everything apart and putting in the exhaust. Then we made sure it fit and marked the last end for changes. We did that at 10pm-3am when it was cool. Then we took pictures and measurements and took it back the next morning. The next week we got it all back but the last piece tack welded with adjustment made. The last piece still didn't fit so we took more measurements and took the last piece back again. A few days later we got it back with changes made in the wrong direction. So we put it back together again measured it and broke the welds on section 4 with a dremmel, ground it all smooth, put it in and placed the last piece in position and marked it with a sharpie. Then today returned to drop it for the final weld and hopefully in a day or two we will have it all done. I an finally see the light at the end of the tunnel with this project.

     I hurt myself during the process grinding down some of section 2 so I was unable to help Sam much with the near final assembly. We have the crossover hoses all cut and in place and the output exhaust hose ready to go as well. Hopefully we can get it all assembled before Friday of this week.

     Two days ago Anamashi took us sailing on their boat and we went snorkeling at the lighthouse reef. Hannah had a wonderful time snorkeling and the water was clear down 15 feet. She swam for over an hour.

     4 days ago the Generator quit working all of a sudden in the morning. That changed the entire day and Sam and I spent the next 8 hours fixing it. Here is the run down. It quit because it overheated. So we started to diagnose the problem. We were outputting plenty of raw water. But we decided to check the heat exchanger. In checking the heat exchanger, which is nearly impossible to reach, I found a broken automotive hose clamp rusted apart. on the input side of the coolant section. Also there was lots of coolant on the floor pan of the generator which we started sopping up. It took me a couple hours to get a new hose clamp on the hose one handed because only one hand would fit. Then we continued to try to figure out what had happend and opened up the input of the raw water side and found quite literally years and 5-6 impellers worth of rubber pieces. Sam suggested flushing it from the other side so we disconnected the anti siphon side of the hose and flushed it with fresh water... even more pieces came out. So we cleaned it all out and sealed it up and refilled the coolant. Then everything worked again... oh my. We were so worried because the generator is so central to everything on this boat.

     Two days ago while grinding off some of the exhaust I cut two of my fingers. This is sooo weird. I've NEVER in my life hurt myself with a power tool but I cut two of my fingers really badly and probably should have had 8 stitches total. I cleaned out everything with a razor, stopped the bleeding put silver into the wounds and superglooed the skin on the top. Then I put a pressure bandage on the wound and splinted it so that it wont open up again. So far no signs of infection and the pain has stopped.

     Last night we spent the evening on Anamashi and today It was He who drove use to Dania beach to drop off the Final piece of the exhaust to be welded.

     It has been very hot and and have been using the air conditioner more now that the generator is working again. When Sam put in the exhaust during thd day on Sunday, we kept the air conditioner running and the ice maker going all day so that we could come in every 1/2 hour or so to cool off. It does not keep the boat cold as it can't keep up but we could come and stand under it for a bit to cool off.

     There will be lots of video on the youtube channel about the work on the generator and the engine/exhaust. The new exhaust actually looks better than the original and instead of brazing with copper this is welded with copper nickle. Sam spent time with a Scotch Bright pad polishing it and it looks wonderful. I know it's a lot to spend and many people feel that what we are doing is not best or cheapest, but I believe it is best for this boat and we are making it better than original with better welding, better materials and improved water flow. The old one lasted 50 years and properly taken care of, I believe that this exhaust will last the life of the boat. It's a piece of art that this Hinckley deserves. As a matter of note, this exhaust if converted to a waterlift would have to lift nearly 7 feet and travel 15 feet to the back of the boat. The exhaust snakes under the floor through bulkheads and lockers where there is no room to do anything else and then rises nearly twice the typical waterlift design height with a huge volume of water to travel 1 1/2 inch diameter for 15 feet. This copper nickle solid exhaust is the best method for this design. I'm not cutting new holes in the hull, I'm not removing or moving exhaust through cabins or cutting new holes in wooden panels. I'm not sending the exhaust through the side of the boat or going out below the water line. And more importantly I'm not testing a new design on a classic boat. I'm not going to have anyone say to me... "what the heck did you do this beautiful old boat!!!??", I'm restoring it.




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